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OCADSAccess DataNDP-064NDP-064 - Notations from At-Sea Notebooks, E-Mail, Correspondence During the Cruise, and the Post-Cruise Analysis of the Data

Notations from At-Sea Notebooks, E-Mail, Correspondence During the Cruise, and the Post-Cruise Analysis of the Data

NDP-064 APPENDIX B

Notations are compiled from the at-sea notebooks, e-mail correspondence during the cruise as well as post-cruise analysis of the data

The following notations are compiled from the at-sea notebooks, e-mail correspondence during the cruise as well as post-cruise analysis of the data. Many of the notations did not have a noticeable impact on the final results, but have been included in an attempt to be thorough. All notations are indexed to 1995 days and are broken down into WOCE leg designations.

Section I8S/I9S

-31.0000   Bob Key set up system in aft port corner of main lab on the R/V Knorr.
           In setting up the computer, Bob blew the fuse on the A/D board. He
           replaced blown fuse with spare located on the board.

-30.0000   Water trap on equilibrator line filled with water. Began official data
           collection at 23:27. Reset run number to 1.

-29.2035   Changed drying column.

-29.3215   Reset computer clock to match GPS.

-29.6875   Ship left the dock. Ken Johnson primary pCO2 analyst.

-28.6895   System water pump shut off...blown circuit breaker on lab plug.

-27.2708   System water pump back on...rerouted to another circuit.

-25.7500   Approximate time of system water pump shutdown due to blown circuit
           breaker.

-24.2500   Replaced air pump.

-20.0000   Frequent system shutdowns due to bow pump failure (caused by heavy
           seas).

-20.0000   Changed to data disk #2.

-19.0000   Changed drying tube.

-17.0000   Refit air pumps.

-11.3300   Seawater supply switched to secondary pumping system.

-10.2500   Ship's bow pump down. 110 power supply for system water pump fried.

-10.7833   Weather up- ship was hove to.

 -7.4181   110 power supply for system water pump repaired by crew.

 -1.0000   Changed to data disk #3. Changed drying column.

  3.2000   Changed to reference tank AAL1791. Notes only stated day...time was
           estimated by examining the data.

  4.7715   Seawater pump down...blown circuit breaker

  7.0000   Changed air pump.

 11.7972   Circuit breaker blown again.

 12.0000   Changed to data disk #4. Changed drying column.

 15.1889   Water pump off again.

 16.0000   Water meter not recording, but water still flowing OK. Changed air pump.

Section I9N

 24.3333   System turned on as ship was leaving port. C. Sabine was primary
           CO2 analyst. While in port, the equilibrator was taken
           apart and cleaned. The shaft bearing on the left side of the
           equilibrator was seized to the disk shaft. It was removed and cleaned
           with steel wool before being replaced (no spare available). Both
           teflon seals were replaced. Discovered that the circuit breaker
           kept tripping on the previous cruise because both the disk motor
           and the water pump were plugged into the same circuit. The two motors
           together can draw 20 amps from the 15 amp circuit. The water pump was
           rerouted to a new circuit. The equilibrator air pump was replaced. The
           water trap on equilibrator air line was replaced with new model.
           Cleaned air filter on line 5. Noticed that CO2 signal was
           very noisy (± 0.01V). Discovered that noise went away if the
           temperature controller was set to 33oC instead of
           35oC. Standard and reference gas use was very high on
           previous cruise, so the standard gas flow rates were adjusted down to
           8-10 mm on the rotometer. The regulator on the 350 standard had
           trouble maintaining a steady flow rate, so it was swapped with spare.

 25.0833   Equilibrator air flow down to 1-2 L/min. Swapped air pumps...flow back
           up to 7 L/min. Have had following wind since leaving port...using aft
           intake.

 27.0000   Wind has come around so it is no longer from behind (intake switched).
           Marine air flow jumped from 1L/min to 8 L/min. Kevin Sullivan (watching
           Weiss system) says Weiss flow is still OK.

 32.1534   Changed perchlorate drying column just before calibration run.

 32.3542   Discovered that marine air rotometer was stuck. After cleaning flow was
           4 L/min.

 33.0000   Marine air flow down to 1.5 L/min. Appears to be some moisture in
           rotometer again.

 34.2431   Bow pump shut off for ~5min. Did not notice whether any samples were
           collected.

 34.9167   Seawater shut off for 15-20 minutes.

 34.9653   Seawater back on.

 35.0076   Bow pump off...switched computer to run gas calibration

 35.0139   Water pump back on.

 35.1625   Changed data disk.

 40.3993   Program paused to change reference tank to ALM008242 (on sta 192).

 40.4313   Program started again.

 40.5000   Paused program to change drying chemicals. Forced to rerun standards.

 47.0000   Examined surface temperature with a bucket and thermometer. Bucket
           temperatures were as much as 1.5  C warmer than CTD temps. I believe this
           represents a real temperature gradient in the upper meter or so of the
           water column while we are experiencing VERY calm, glass-like conditions
           and bright sunny days.

 47.9590   Changed data disk.

 50.8611   System water pump quit and drained equilibrator.

 50.8646   Water pump back on.

 50.9076   Water pump quit again.

 50.9306   Water pump on again.

 51.8889   Water pump out 1-2 minutes.

 51.1229   Water pump out 1-2 minutes. Believe pump brushes are worn out.

 51.4028   Changed drying chemicals. Forced to run calibration.

 53.2000   Started run East to Andaman Islands to drop off observers.

 53.3958   Water pump swapped with spare while system was running standards. Checked
           old motor and discovered centrifugal switch was warn out.

 58.0000   Changed data disk.

 59.1471   Stopped program and installed PCO2A3.BAS. This program reads the IMET
           data in real time. While system was down, the drying chemicals were
           changed and cleaned the equilibrator rotometer (6).

 59.2134   System up and running again.

 59.4316   Program crash due to garbage in IMET signal.

 59.7271   Program crash.

 59.8542   Program crash.

 60.0604   Program crash...switched back to PCO2A2.BAS until error trap
           can be written.

 60.3104   Started PCO2A3.BAS

 60.3403   Program crashed...fixed.

 60.7674   Marine air pump replaced.

 62.0104   Program crash.

 62.4109   Program crash.

 62.4894   Program crash.

 63.3022   Bottom of drying column very wet. Stopped program and changed chemicals.
           Nafion tube seems OK...must have been some plug of water blown through?

 63.4295   Program crash.

 64.1007   Shut water flow off. Running final standards.

 64.1250   Program stopped.

Section I8N/I5E

 69.5366   System started after Knorr's departure from Sri Lanka (G. McDonald in
           charge).

 70.3021   Noticed water in perchlorate drying column. Replaced Nafion tube, fixed a
           clog in Ultra Torr tee on perchlorate column and changed drying chemicals.

 71.0010   Marine air pump replaced.

 71.1563   Detector voltage seemed "spiky" on standards, lowered rack temperature
           controller to 32.5oC.

 74.3021   Reset all flow rates based on standard tank pressure dropping. IMET data
           flaky. System had to be restarted.

 77.2500   Power shutdown in main lab...system off-line.

 77.4167   System restarted after power was restored to lab.

 78.0243   Marine air pump replaced.

 82.0000   Post cruise analysis of data indicates that the time spent trying to
           analyze the standards is starting to get significantly longer. The reason
           for this is not known since Gerry did not notice this while the system was
           running, but we suspect that the system got noisy again most likely due to
           the continued degradation of the timing LED in the detector. The problem
           does not seem to have affected the data quality, only the length of time
           it takes the detector to stabilize and thus the quantity of data collected.

 88.4500   Estimated time when reference tank was changed (Gerry's notes somewhat
           ambiguous). New reference tank number ALM027282.

 97.8681   Ship's bow pump down...rough weather.

 97.8743   Bow pump running again.

101.0000   Equilibrator air supply low...adjusted back to proper setting.

103.3354   System locked up due to shutdown in IMET data, Rebooted computer at
           103.4694.

104.7500   Ship's bow pump shut down upon approach into Fremantle.

Section I3

106.0000   Swapped detector for LiCor replacement. Broke rack temperature controller
           PRT, replaced with spare.

113.0040   Departed Fremantle, Australia (R. Key running system).

113.6042   Reversed course for medical drop off.

114.0618   Rack temperature controller set temperature lowered from 32.5 to 30.5oC.

114.1562   Reversed course after medivac.

115.0833   Changed pump heads and changed drying column (started using Aquasorb in
           drying column instead of Mg-perchlorate).

116.0784   Complete cleaning of equilibrator air lines up to Valco, clean pump, new
           drying chemicals. Flow greatly improved.

118.0208   New drying column.

119.0001   Data transfer.

120.0799   New drying column.

122.1507   New drying column.

124.5986   New drying column.

126.6153   New drying column.

127.0146   Data transfer.

127.6674   New drying column.

129.7139   New drying column.

132.1500   Cleaned equilibrator pump.

132.3785   New drying column.

134.0604   Data transfer.

134.7882   New drying column (started using 1/2 Aquasorb and 1/2 Mg perchlorate in
           drying column).

137.0000   Lost prime on bow pump several times for a few minutes- (.2882- .2910,
           .4444-.4514, .4549-.4618, .6389-.6479, .7243-.7264)

139.0417   Lost prime on bow pump - restarted 139.0514.

139.7500   System crash due to IMET error - program restarted.

140.4319   System shutdown for 20 min. to check on axle squeak.

141.3549   New drying column.

144.2062   Changed reference tank to ALM14400.

145.4924   Bow pump off approaching Mauritius.

148.1771   Restart program departing Mauritius.

149.4604   Data transfer.

150.4882   New drying column.

151.2083   Swapped leaky reference gas regulator.

154.4465   New drying column.

156.0583   Seawater shut off for final approach to Mauritius.

Section I5W/I4

162.1900   Set sail from Mauritius.

164.2431   Changed drying column.

166.2882   Adjusted all reference and standard gas flows to get system in balance.

167.6321   Noticed some shredded PVC around axle seal - discovered that axle bushing
           had seized to shaft and was rotating in PVC endplate. Shut system down and
           took apart equilibrator. Had to get ship's engineers to remove bushing and
           epoxy spare into endplate.

168.3875   System running again after equilibrator repairs.

168.4826   Data transfer.

168.7521   Changed drying column.

171.7236   Changed equilibrator air pump.

172.1475   Stopped system on approach to Durban.

173.3401   Restarted system after leaving Durban.

174.7500   Bow pump off for 9 minutes. Seas have been fairly heavy for several days.

175.1667   Bow pump off and on several times since first shutdown.

175.6236   Changed drying column. Made small adjustments to flow rates.

182.1972   Data transfer.

182.8472   Very rough seas (Swells 15-20'). Bow pump has been off and on. Decided to
           just run air until things calm down a little.

183.5555   Weather has calmed down a little...bow pump back on line.

184.0000   Have been getting bow pump shutdowns while on station. Small water leak
           through axle seal...adjusted equilibrator float switch down to lower water
           level.

185.6667   Changed drying column and data transfer.

188.3757   Changed equilibrator air cadet.

190.4583   System crash due to IMET problems - rebooted. Data transfer.

191.9271   Bow pump shutdown for approach into Mauritius.

Section I7N

196.3125   Departed Mauritius (T. Zahn in charge).

200.6250   Changed drying column. Have had rough weather for past couple of days.

201.0000   Not getting proper sample flow through system ever since changing drying
           column. Tried all day to find problem...finally discover that the drying
           column was not being sealed with the O-ring.

203.0000   Data transfer.

205.1875   Bow pump shutdown for repairs...back on at 205.2417

206.4868   Changed to reference tank 24813 (note: this tank is a zero CO2
           gas, started with only had 700 psi).

206.4868   System crashed...when rebooted system was told to run partial standards
           (note: this option was not supposed to be used, but should not have a
           noticeable affect on the calibration).

208.5625   Data transfer.

215.6944   Drying column changed.

217.6174   Data transfer.

219.1153   Changed partial standard collection off.

220.8472   Program crash...system rebooted.

221.0000   Bow pump off and on several times during day. Some water leaking through
           teflon seals.

222.0000   Still having problems with bow pump.

226.0000   Bow pump shut off a couple times during the day...water leak getting worse.

227.3958   Changed reference tank to 18260 (a zero CO2 standard).

228.0000   Weather very rough...switched to secondary seawater pump 228.4236.

230.3813   Seas calmer...switched back to regular bow pump.

233.6285   Data transfer.

235.3979   Bow pump shut off for approach into Oman.

Section I1

241.4167   Ship sailed out of Oman (R. Rotter in charge). Equilibrator was taken apart
           and cleaned. Shaft bushing was replaced and epoxied into endplate. Replaced
           teflon seals and bypass chamber with spares. Equilibrator PRT and float
           switch were broken in rebuild and had to be replaced with spares.
           Collection software was replaced with newer version. Collection scheme was
           basically the same as the original software, but version had slightly
           different display and more error trapping.

241.9055   Data collection began.

243.5000   Wind and swells up - bow pump off and on.

243.8917   Drying column changed.

244.8403   Bow pump off. Resumed at 244.8458.

245.0000   Bow pump frequently shutting off all day.

245.6035   Stopped program temporarily to reset standard flow rates.

246.1632   Bow pump off. Resumed at 246.1764.

247.4938   Drying column changed. Data transferred.

248.0215   System set to run partial standards.

248.6618   Power outage - system reset

250.8000   Drying column changed.

251.7194   System reset so it would not run partial standards.

253.1806   System crash due to bad IMET data.

253.0000   Weather getting rough again water pump off and on all day.

253.9000   Drying column changed.

254.4708   Data transferred.

255.6479   Adjusted equilibrator air flow rate.

256.1167   Adjusted equilibrator and marine air flow rates.

256.9118   Drying column changed.

258.0417   System crash due to bad IMET data.

259.0660   System water pump off. Restarted several times, but ultimately had to
           replace water pump motor with spare.

259.9410   Drying column changed.

260.6160   Data transferred, program restarted.

262.9420   Drying column changed.

263.5208   Marine air pump off. Replaced 263.5347

263.7083   Marine air pump off. Replaced 263.7291

264.0000   Weather very hot...noticed that box temperature frequently getting above
           set temp.

265.5458   System crash due to bad IMET data.

266.7132   Drying column changed.

269.5174   System crash due to bad IMET data.

269.9999   Drying column changed.

271.0556   Bow pump off approaching Sri Lanka.

273.8597   System started after leaving Sri Lanka. Changed set point for rack
           temperature controller from 30.5 to 31.5 since rack temp has been getting
           above set point since day 264.

276.8667   Drying column changed.

278.6319   System crash due to bad IMET data.

279.9083   Drying column changed.

281.9736   Data transfer.

282.7840   Drying column changed.

285.4097   System Crash -unknown error.

285.4215   Diskette had bad sector...had to replace with new diskette. Reset system,
           adjusted flows and changed drying column.

286.1215   Bow pump off as ship enters straits of Malacca. Restarted program without
           IMET data and ran full standards.

286.4145   Shut down system. Discovered that hard disk was full from 10/7 to 10/13 -
           Recovered data from floppies. IMET data recovered from ship's 1 minute
           files.

Section I10

303-313    C. Sabine and G. McDonald cleaned bypass chamber and equilibrator. It was
           reassembled with new teflon seals and cleaned bushing. Rebuilt seawater
           pump...replaced old impeller and link belt. Replaced reference gas with
           cylinder ALM061635 (new calibrated 200 ppm CO2 standard).
           Transferred all data files off of hard disk. Adjusted zero setting on
           detector to give 0.1V reading on reference gas. Adjusted rack temperature
           controller back up to 35oC so it could properly maintain
           temperature. System tested on transit from Singapore to Australia. Knorr's
           ET was aboard making changes to IMET system, so pCO2 program
           was modified compensate.

315.2943   System started after leaving Dampier, Australia (G. McDonald in charge).

316.0833   K. Sullivan adjusted main water flow for CFC syringe bath.

316.1388   Bow pump off and on 5 times over next 5 hours (choppy seas).

317.1056   Bow pump off and on 3 times over next 2 hours.

319.5243   System crash - system rebooted.

320.2208   Exited system to confirm data was being collected properly.

321.1097   Changed drying column.

322.2250   Transferred data.

323.2215   Noticed that CO2 concentration signal was noisy. Looked at long
           term trends and determined that noise started around day 322.5. The noise
           was due to erratic pressure readings because the 4 pin molex connector was
           loose. Reconnected plug and signal returned to normal.

323.2674   Changed equilibrator air pump.

324.2260   Changed equilibrator air pump to a quieter one.

325.2180   Changed drying column.

329.0104   Bow pump shutdown entering Indonesian EEZ.

Section I2

339.2764   Data collection started after leaving Indonesian EEZ.

342.2319   System crash due to bad IMET data.

342.9861   System crash due to bad IMET data.

344.3833   Changed drying column.

346.9721   System crash due to bad IMET data.

348.4665   System crash due to bad IMET data.

350.8927   System crash due to bad IMET data.

352.9182   System crash due to bad IMET data. Data transferred.

354.9312   System crash due to bad IMET data.

359.0511   System crash due to bad IMET data.

361.5194   Bow pump shutdown entering Diego Garcia.

364.0000   Changed reference gas tank to ALM45918. Had trouble getting reference gas
           flow down to correct rate (flow is 15 and should be 8-10).

364.3583   System restarted leaving Diego Garcia.

366.9705   System crash due to bad IMET data.

367.6049   Rebuilt needle valve controlling reference flow rate and finally got the
           correct flow. Standard fits have not been very good for past few days
           while reference flow was out of whack.

371.8229   System crash due to bad IMET data.

377.3785   Bow pump shutdown for 5 minutes.

377.6468   System crash due to bad IMET data. Readjusted gas flows.

378.6762   System crash due to bad IMET data.

380.6441   System crash due to bad IMET data.

383.6758   System crash due to bad IMET data.

386.6076   Final shutdown approaching Mombasa. Final water flow meter reading
           1,146,780 gallons!
Last modified: 2021-03-17T18:30:27Z